Innovative Foundation Solutions Save the Day

Author: EMILIO M. MORALES, MSCE (Principal)
Organization: EM2A Partners & Co.
Address: QUEZON CITY, PHILIPPINES

ABSTRACT

Foundation problems abound and sometimes solutions to various foundation problems could result in costly procedures or measures in order to remedy the problem. Introduction of Innovative Solutions to problems in Foundations together with a clear understanding of the problem and application of Innovative Technologies result in cost effective solutions. Two case studies are presented in this paper to illustrate such solutions.

Key Words: Underpinning, Ground Improvement, Jet Grouting, Rammed Aggregate Piers, Geopier®, Settlement Ground Vibrations

INTRODUCTION

The subsurface soils being natural deposits tend to introduce unexpected variability in the subsoil that is not revealed by the soil exploration or during construction. This situation could lead to costly delays in the process. In addition, errors in construction of foundations could lead to serious problems that would require costly intervention.

This paper addresses the foregoing real world problems, which have been solved with the use of innovative foundation technologies.

Two (2) case studies are discussed to illustrate the measures and solutions employed to solve the problem.

CASE I – SETTLEMENT OF BORED PILE FOUNDATIONS

A pier supporting 60 m long span Precast concrete Box Girders for a light rail transit line crossing a river experienced significant settlement immediately upon placement of the Girders (Dead Load).

This initial settlement of 36mm caused concern and was continuing progressively until loading and other construction activities were halted. At that time, a total of 45.7mm maximum settlement has already resulted.

The erection subcontractor for the Precast Concrete Box Girder segments specified a short-term maximum settlement of 30mm and a total long-term maximum settlement of 45mm.

The initial settlements have actually exceeded these values and the Box Girders have to be relevelled by jacking in order to level the Girders. All construction activities were halted at this juncture and intermediate heavy steel supports were placed near the Pier support in case further settlements are experienced.

Our organization was engaged by the Contractor initially to undertake an investigation of the subsurface to determine the possible cause/s of the settlement which was very alarming considering that this particular Pier is supported by six (6) large diameter Bored Piles on a massive pile cap.

The following are the details of the Bored Pile foundation:

Number of Bored Pile N = 6

Diameter of Bored Pile D = 1500 mm

Length as installed L ] = Varies

Theoretical Allowable

Load bearing Capacity (MT) ]

CStatic = 515.46 MT/pile
CEqk = 799.69MT/pile

The design called for embedment into soft Bedrock of 1.0 to
2.0 meters depending on whether the Bored Pile embedded length is long or short (> or < 10.0 meters).
Two check Boreholes were drilled, one at the toe of the Pile
cap and another near the edge of the column close to the middle Bored Pile.

The check Borings (Fig. 1.0 below) indicated that the overburden soils are relatively poor to very poor beyond 7 meters as shown in the Soil Profile below for BH-1 and BH-2.

Fig. 1 – Soil Profile near Pier Foundation

As can be seen, refusal was only encountered at a depth of 15.12 meters and 14.40 meters below existing Natural Ground Line.

A tabulation of the drilling results when matched against the installed depth is shown below:

Fig. 2 – Tabulated Values of Bored Pile Lengths

As can be seen from the above, two of the Bored Piles (BP-1 and BP-2) were literally resting on very soft clay and the rest were socketed only about 0.24 meters into the possibly highly weathered Soil/Bedrock Interface.

The RQD values below the soil bedrock interface showed relatively fair values of 19% and 16% respectively.

Bedrock Unconfined Compressive Strengths are about 20.0 kg/cm2 near the Bored Pile Tip characteristic of soft rock known as the Guadalupe Tuff Formation (GTF).

Thus, the heavily loaded Bored Piles were either resting on very soft clay or on relatively weathered Bedrock very near the Soil Bedrock interface without adequate socketing.

The remaining gap is about 10mm after the recorded settlements. Thus, it was possible that the clays have been squeezed out at some locations resulting in the Bored Piles resting partly on the Bedrock and partly on very soft clay.

This is the primary cause of the relatively large settlement that was experienced at this particular Pier location.

Geology of the Site

The site across the San Juan River in San Juan, Metro Manila is generally underlain by the Guadalupe Tuff Formation (GTF), a massive suite of soft Tuffaceous Volcanic rocks.
The Pier Foundations that settled supported the Eastern end of the 60 m long girders spanning the river.

Overburden soils are relatively poor to very poor below 7 meters and consist of clays and silts down to about 15.0 meters and sloping towards the San Juan River.
The thick and very poor overburden needed to be bypassed by Bored Piles to transfer the foundation loads to more competent rock.

What Caused the Settlement?

The Bored Piles were not adequately socketed as required and were partly resting on very week materials. It was possible that boulders and large cuttings were encountered which resulted in erroneous interpretation that the Bedrock level had been penetrated.

As stated earlier, the specification called for a minimum socket depth of 1.0m to 2.0m into bedrock. No clear or reasonable explanation could be given as to why the Bored Piles were installed short of the target depth. It can only be assumed that this was overlooked during the installation and the hole was not cleaned or inspected at all.

The Jet Grouting solution was finally selected because it offered a far better assurance of stability during seismic loadings. As shown in Fig. 3 the solution consisted of providing a Jet Grouted Wall around the footprint of the Pile Cap and at several interior locations as shown in the plan.

This Jet Grouted Curtain Wall in Secant Pile arrangement would assure full assumption of the load from the Bored Piles while at the same time increasing resistance to sliding and overturning.

Fig. 3 – Settlement History

Remediation Measures

Immediately upon detection of on-going settlements, formal settlement monitoring and recording was started 27 January 2001. Because of continuing high rate of settlement, construction loading was halted on February 28, 2001. Heavy Structural Steel scaffolding was placed to support the Girders and Jacking releveled the Girders. Still settlements continued but at a reduced rate resulting in a total of 45.7mm settlement of the Pile Cap.

The ensuing check borings (Fig 1.0) verified that the Bored Pile tips were resting on very soft soils or on highly weathered bedrock.

Several remediation measures were discussed and these were narrowed down to two feasible technologies:

Fig. 4 – Section showing remediation procedure
Fig. 5 – Jet Grouting Machine set up under Pier
Fig. 6 – Jet Grouting Equipment Layout
Fig. 7 – Layout of Remediation using Jet Grouting

In addition, each of the Jet Grouted Piles were reinforced at the center by 25mm Ø rebars which were inserted by redrilling the Jet Grouted Piles (JGP) and extending 2.0 meters beyond the Soil/Bedrock interface into competent Bedrock. The drilled hole and dowel bar were subsequently regrouted effectively doweling each JGP into the Bedrock. Expansive admixture and higher strength mix was used to grout the rebar to the Pile Cap. This provided extra shear capacity over and above that provided at the Pile Cap/JGP Interface.

The settlement record for the project is shown in Fig. 3. The milestones are flagged. It can be seen that with the initial Jet Grouting, additional settlement of 19.3mm was experienced due to further disturbance of the weak soils near Bored Pile Tips, although care was exercised to reduce such disturbances to the minimum by initially drilling far from the Bored piles. The Girders had to be releveled again by Jacking.

The Jetting was halted to allow for the curing of the Soilcrete and also because questions were raised about the effectiveness of the technology given the additional settlements. After Field trials were done to verify the effective diameter of the JGP and the Guaranteed Compressive Strength it was shown that the Test Piles satisfied or even exceeded project requirements. Subsequently, Jet Grouting was restarted for the final Jet Grouting of 38 Piles on November 1, 2001. Only 10mm additional settlements were recorded. The Jet Grouting was completed on December 12, 2001.

Although the Jet Grouted Curtain wall would be more than adequate to support the total foundation loading, the Project consultants required that the existing Bored piles be redrilled at the center to allow for the insertion of Grouting equipment in order to grout the pile tip. This would ensure that once the “Soilcrete” has cured, the Bored pile tips would be resting on solidified ground. This was accomplished after the initial JGP installation and was done initially in areas where the JGP have substantially cured and attained full strength.

The solidification at the tip of the Bored pile is shown in the figure below:

Fig. 8 – Bored Pile Tip Detail After Grouting

No further settlements have been recorded despite the placement of ballast and rail tracks as well as other hardware and the remediation was considered successful.

Lessons Learned

Careful monitoring of the Bored Pile installation is very important to ensure the integrity of the Bored Pile foundation including adequate and proper cleaning of the bottom from cuttings and degraded rock. It is also important to ensure that the specified socket depth is attained.

The innovative remediation process instituted successfully arrested the settlements and restored the Pier to full serviceability.

CASE 2 – WAREHOUSE CLUB ON VERY POOR SOILS

A 6,500 square meter retail warehouse was to be constructed on very poor swampland soils originally used as a precast concrete plant yard.

The original solution called for Driving of R.C. Precast Piles to support the warehouse including the Warehouse floor, as anticipated settlements would result in cracking of the heavily loaded floor. The suspended structural floor supports merchandise racking with a distributed load of about 450 psf. The levelness of the floors is critical for the safe operation of the medium reach forklifts used in the warehousing operations.

However, during the initial Test Pile driving, complaints were received from the neighborhood residents due to large vibrations experienced as well as damage due to cracking of walls in several houses.

The damage was due to soft ground amplification of the pile driving vibrations. Work had to be halted indefinitely until a substitute could be proposed. The only alternative was to use Bored Piles. In order to optimize and mobilize the full capacity of the Bored Piles, the Bored Piles would have to be deep and the loads concentrated onto a limited number of Bored Piles. This, in turn, required heavy structural framing systems consisting of Deep Girders and Beams to carry the heavily loaded Warehouse floor and transfer the loads to the Bored Piles. The resulting cost of the Bored Pile foundation and heavy floor framing system was estimated at P45.0 Million.

Value Engineering Alternative

Our company offered a value engineering alternative using Geopier® foundation. The proposed solution consisted of installation of about 1900 Geopier of 3.0 to 3.5 meter length supported on the very soft soils. The Geopier foundation system is a Rammed Aggregate Pier system using patented technology. Installation is done in the following sequence shown by the fig below:

Fig. 9 – Sketch of Geopier® installation procedure

Due to the installation procedure, which consisted of ramming the aggregates using a patented beveled rammer, lateral prestraining and precompaction of the surrounding soils were realized. This prestraining and prestressing effect resulted in significant increases in lateral stresses around the Geopier perimeter resulting in very significant stress transfer by skin friction to the surrounding soils. Only very minimal residual stresses due to the loading were transferred to the Geopier tip thus resulting in large reduction in settlements of the Geopier.

The columns were supported on two or three 3.5 meter Geopier. Columns supporting Canopies requiring uplift resistance were supported on tension Geopier, which were reinforced with, rebars restrained near the Geopier tip by steel plates.

The suspended structural framing Support of the merchandise and warehouse floor was totally eliminated. In its place, a very innovative slab support system was substituted. The slab support system consists of a 1.0 meter thick Engineered Granular fill supported on Geopier at 3.0 meter on centers by arch action. The arch action transfers the entire load onto the Geopier elements. This enabled the floor slab to be designed as a conventional slab on Grade with reduced reinforcement and with very minimal settlements.

Fig. 10 – Sketch showing slab support using Engineered
fill to transfer floor loads to Geopier by Soil arching.

This value engineering alternative was considered only after written guarantees secured by a USD 500,000 liability insurance was issued by our US Principals to limit the settlements to within 20mm.

However, this innovative solution presented several advantages to the owner as follows:

  • Reduction in foundation installation time
  • Reduction in overall construction time by elimination of a structural floor system.
  • Significant cost reduction due to the high cost of Bored Piling as well as the integral structural floor framing system.

Furthermore, it was stipulated that we have to perform an actual Field Installation demonstration with the Village Association Officers in attendance in order to convince them regarding the minimal vibration and noise resulting from the installation and also to ensure that no damage will result from such activities.

This was successfully done and the contract was awarded to the company.

Modulus Load Test

As part of the execution, a Modulus load test was performed on a production Geopier in order to determine the settlement under the full service load. The Geopier Modulus test is similar to the setup used in a pile load test but the interpretation is different.

Fig. 11 – Modulus Load Test Graph

The Stiffness modulus values of installed Geopier elements are determined by full-scale modulus tests. The test is performed by applying pressure in gradual increments over the full cross-section area at the top of a Geopier element. The stiffness modulus value corresponding to 100% of the design stress applied to the top of the pier is determined based upon the load test results, and is typically expressed in English units as pci, and in metric units as MN/m3. The Geopier modulus load test is not a bearing capacity type test, such as a pile load test. Rather, it is a settlement test to determine a conservative value of pier stiffness. The Geopier foundation system design uses the stiffness modulus value measured at the point of maximum anticipated design stress; i.e., at 100% design top of Geopier stress (or at the maximum acceptable deflection) from the modulus load test results. Geopier modulus tests are normally performed to a top of Geopier stress equal to 1.5 times the maximum design stress. The purpose of applying load to more than the design stress is just to observe the Geopier element deformation characteristics at higher stress levels.

The results of the Modulus load test for this specific project is shown in Fig. 12 below:

Fig. 12 – Modulus Load Test Results

As can be seen from the above a total of only 0.218mm settlement was obtained under full service load and that failure was not reached at 1.5 times the maximum service load. A residual settlement of only 0.231mm was left after unloading of the Modulus test.

The installation was done at the height of the Typhoon season but the project was completed on time.

As a result of this Value Engineering alternative, the construction time was shortened by two (2) months allowing for an earlier opening of the Warehouse club. This was because the heavy suspended floor was totally eliminated and the floor was designed as slabs resting on a compacted engineered fill instead. The engineered fill in turn is supported on Geopier spaced at 3.0 m on centers by arch action.

The construction sequence also was favorable to the General contractor as the GEOPIER procedure allowed immediate work to be undertaken immediately after a section has been completed. Critical time waiting for the curing of piling etc was totally eliminated. Compaction of the engineered fill was started at sections adjacent to Geopier installation activity without the possibility of disturbance to the engineered fill. Pouring of the concrete slab on grade immediately followed the completion of the engineered fill compaction. At any given time, concrete pouring was about two bays distant from any Geopier installation activity, thus vibrations are no longer a critical issue during the curing of the concrete.

This also resulted in a savings of about P 20 million over that of the cost of bored piling and suspended structural floor system.

The project was completed two months ahead of the original scheduled date of opening and the overall savings due to this value engineering solution was very significant.

Lessons Learned

Pile driving on very soft soils can cause amplification of harmful vibrations, which could damage adjacent structures. In addition, breakages of driven concrete piles during driving are possible due to the setup of tension waves from rapid pile driving. Costly suspended floor systems can be eliminated with the use of innovative solutions for load support.

Conclusions

The foregoing are but two of many available solutions to solve day-to-day Foundation problems innovatively. The two cases also illustrate what can go wrong in a project, which may require the use of new or innovative technologies to solve the problem effectively.

] Based on Piling Contractor’s Bored Piling record.
] From Capacity Calculation Sheets.

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Investigation of Cracking of a Large Area Wear Slab – Lessons Learned

Emilio M. Morales, MSCE

ABSTRACT: A large area wear slab was designed as a jointless wear slab. Originally specified with shrinkage compensating concrete (SCC). The slab was poured as an ordinary PCC concrete with temperature rebars due to non availability of SCC.
The wear slab is underlain with two layers of 300 mm thick Expanded Polystyrene EPS which turned out to be substandard.
Subsequently, approximately two months after pouring, severe cracking and dusting occurred. The cracks were predominantly spiderweblike cracks and also manifestations of shrinkage induced parallel cracking.
An investigation was requested by the Owner from the Engineer and two Third Party Engineers. This was followed by a report from the EPS supplier commissioned Engineer. The latter laid the blame almost entirely on the Prime Contractor and the Engineer.
The ensuring debate resulted in a three cornered fight between the Owner/Engineer, the Prime Contractor and the EPS Supplier.
This paper presents the Engineer’s own investigation and the final outcome of the problem.
The paper is good reading for Engineers and Contractors alike who face or are likely to face litigation due to construction problems.

INTRODUCTION

A large area Dairy Products Warehouse approximately 1.4 hectares covered area required that the wear slab on the Refrigerated Warehouse areas be of jointless construction for reasons of sanitation and hygiene.
The slab was specified to have a maximum water cement ratio of 0.42. This would result in a minimum concrete compressive strength fc’ of 35 MPa (5,000 psi).

The wear slab is underlain by two layers of Expanded Polystyrene (EPS) supported in turn by a structural slab on grade. The slab on grade rests on well compacted gravel base course on compacted subgrade.

Figure 1.0

The wear slab was originally proposed to be poured using Shrinkage Compensating Concrete (SCC). However, due to non-availability, this was not possible. The Engineer then specified the use of Fly Ash in order to reduce the heat of hydration and also the water demand. However, the contractor certified to the non availability of Fly Ash at that time. As a result, the Owner ordered the pouring of the slab without SCC or Fly Ash.

The slab was required to be poured only after the roofing and cladding have been installed to protect against the weather.
Two months after pouring, the slab exhibited cracks that were predominantly spiderweb-like but also manifested parallel cracks characteristic of shrinkage cracking.

In addition, and after the warehouse was made operational, severe dusting in some areas posed a critical problem.
The dust was being recirculated by the ducted airconditioning system causing discomfort to personnel and also as a potential source of contamination to the dairy products.
As a result the Owner, in consultation with the Engineer of Record provided an overlay slab. The overlay slab sealed the old wear slab and supplanted the cracked wear slab which provided the permanent solution.

However, the Owner wanted to pin responsibility and even before the plant was placed in service, investigations have been conducted. The results of these investigations, the final conclusions and how the problem was identified and resolved are the topics of this paper.

NATURE OF CRACKS

The cracks were detected in various areas of the refrigerated stores and manifested themselves as spider web like in appearance within depressed areas. Also, parallel transverse cracks about 0.5m to 3.0m in length were detected in various areas.

The cracks only occurred in the refrigerated areas which is underlain by EPS.

INVESTIGATIONS MADE

Investigation by Engineer of Record

The Owner initially requested the Engineer to conduct an initial investigation to determine the cause/s of the cracking in the refrigerated area and to make necessary recommendations on the remedial measures needed to restore the slab to its functional serviceability.
Due to the preponderance of dishing patterns marked by spiderweblike cracks, the Engineer of Record focused on subgrade failure or settlement as the cause. However, structural calculations were also made to check that the slab would be adequate for the forklift loads imposed. This was verified to be adequate based on Westergaard analysis treating the EPS as the subgrade.

Subsequently, destructive investigations were ordered by the Engineer which consisted of:

  1. Concrete coring on the wear slab for Unconfined Compression Tests.
  2. Large diameter coring of the EPS to determine the density (and the modulus by correlation with density) and load at 10% deformation.

The results showed that:

  1. The concrete was grossly understrength.
  2. The EPS is substandard and very much below the specified density of 32 kg/cu.m.1] and the modulus was also low.
Figure 2.0

The EPS supplier made similar and parallel tests which essentially corroborated the Engineer’s test results and clearly established that the concrete and EPS were both substandard.
Although the foregoing results initially addressed the issue, the shrinkage cracks can not be explained by these findings and additional studies were needed.

Independent Local Consultant

The Owner then also hired an independent local Consultant who concurred right with the Engineer of Record’s findings in a meeting attended by all parties.

Independent American Consultant

Not content with the foregoing, the Owners foreign Joint Venture partners hired a second independent Consultant who, after visiting the plant and seeing the cracks immediately concurred that it was subgrade failure due to the compressibility of the substandard EPS.

He stated in his report and we quote: “Based on information presented to this office to date, it is our opinion that the cracking problem was caused by failure of the Polystyrene Foam insulation to meet project specifications”.

The Owner was ready the slap claims for damages on the EPS Supplier.

EPS Suppliers Consultant

As a defensive measure, the EPS supplier recommended a Third Independent Consultant from New Zealand to prepare a report. The Owners and the Engineer agreed to this suggestion for the sake of fairness and to show good faith.
The results of this EPS Consultants findings and recommendations came as a shock to all as it overturned all the previous investigations and findings completely. This report and its conclusions needed to be discussed at length as the ensuing response to these conclusions established the actual problem and solution.
The report by the EPS Supplier’s Consultant laid the blame squarely on the Prime Contractor and the Engineer and almost dismissed the responsibility of the EPS Supplier for substandard products by a slap on the wrist.

Fortunately, this report was proven to be flowed as it made conclusions on the basis of numbers or figures which could not be supported by calculations. How this was done is the main purpose of this paper. The procedures employed by the Engineer in doing so lays the groundwork for resolution of similar problems and avoidance of litigation.

The New Zealander Consultant hired by the EPS supplier concluded that:
The cracking was mainly due to shrinkage and it identified the following as the major contributing factors to the shrinkage 2]:

⦁ “Inadequate shrinkage control measures in the floor slab design.
⦁ Excessive water in the concrete mix causing shrinkage of up to four times what would have been expected from the specified mix

While recognizing that the “underfloor Polystyrene Supplied is below specified density” this observation was not pursued further in terms of its contribution to the slab cracking!
The EPS Consultants report totally neglected the contribution of the very low subgrade support offered by the substandard polystyrene supporting those slabs despite the crack patterns and also ignoring the conclusions of two other Independent Consultants attributing the cracking to the substandard EPS.

It also recommended an arbitrary apportionment of liability that pinned the responsibility mainly on the Designer and Main Contractor.
While the EPS Consultants report was flawed because it made general conclusions without having any basis or calculations to support these, it also proved that:

  1. The as laid concrete had a very high water cement ratio (W/C = 0.833)3] which is almost double the specified water cement ratio (W/C < 0.42).
  2. It supported the findings on the core strengths obtained.

REVIEW OF THE EPS CONSULTANTS FINDINGS

As earlier stated, the report caused some shock and alarm to the Owner and as the Engineers we were asked to comment on this report.
Our review of this report showed that:

  1. The report was flawed because it predicted the strain on the as designed slab as 0.350mm/m (350 millionths) which later on turned out to be unsupported by any calculations!
  2. The report dealt with qualitative assessment that was based on generalized assumptions leading to erroneous conclusions particularly on the assignment of responsibility.
  3. The EPS Consultant concluded, unsupported by engineering calculations, that the concrete wear slab as designed and as-built would have cracked in the same manner. This erroneous conclusions is due to their failure to quantify by calculations the shrinkage strains which would result from the as-designed and as-poured mixes. This is due to the non recognition of th shrinkage control measures specified by the Designer which included:
    • Control of W/C to 0.42
    • Limiting slump to 2 inches (50mm)
    • Increased strength of concrete to 5,000 psi minimum by specifying W/C to be 0.42 maximum.
    • Shrinkage control rebars
    • Extended curing period of 14 days by ponding
    • Specified use of SCC or Fly Ash (which was not carried out with the knowledge of the Owner)
    • Requirement for full enclosure before pouring of slabs.

The EPS Consultant would cursorily dismiss these measures no being “insufficient” (based on a letter dated 15 February 1997).

Herein lies the crux of the matter because we shall prove subsequently, and supported by calculations, that the measures specified were more than adequate to control cracking.
Thus, although it resulted in countless hours of engineering time and research, the study was worth it for it clearly proved that the specifications were adequate to prevent cracking despite the non use of the originally specified SCC or even in the “absence” of Fly Ash.

It also emphasizes the fact that sound Engineering can always stand on solid ground and rely on Fundamental Engineering Principles despite efforts to mask the truth.
The EPS Consultants report was proven without basis and is flawed because it can not support its shrinkage quantification of 0.350 mm/m in the light of our calculations showing that the shrinkage strains resulting from the as- specified concrete mix was well below the critical threshold strain magnitude for cracking to start (0.200mm/m or 200 millionths).

SUMMARY OF TEST RESULTS

The tests on concrete and EPS cores are included as Table “A” and Table “B” in Appendix “C”. In addition, the water cement ratio on the hardened cores as performed by BRANZ showed that the W/C Ratio is 0.833 average. These tests results already clearly established that the materials as used were substandard and grossly non complying with the specifications.

CALCULATIONS AND QUANTIFICATION OF SHRINKAGE STRAIN MAGNITUDE

The Methodology and procedures employed strictly followed the universally accepted ACI 209R-92.
The calculations showed that:

  1. Although the ultimate strains εsh were 290 millionths and 1020 millionths for the as-specified and as-poured concrete smaller values were obtained when various correction factors are applied as provided for in ACI 209R-92. The large disparity is in the very high Water Content of 47.9 gals/CY for WC 0.833 for the as poured concrete.
  2. Shrinkage correction factors were equally applied for the as- specified and as poured concrete mix. The product is 0.3654 the resulting strains are:

3. The environmental and other considerations are very important in quantifying shrinkage strains and whether such conditions would cause cracking of the slab.

4. These environmental and other factors and their contribution and effect to the shrinkage magnitude are very important and highlight the fact that shrinkage can be controlled by controlling these factors.

The calculations and references are included in this paper as an appendix as a guide to the reader.

CONCLUSION

As a result of the foregoing findings and computations, the EPS supplier’s consultant did not anymore respond nor repute the results of our studies.
The EPS supplier and the main contractor entered into a compromise agreement with the Owner and the Engineer of Record was totally cleared of any responsibility or liability.

1] Since the compressibility modulus of the EPS (Ey) can be directly correlated to the density [Horvath], the settlement of the EPS can be predicted.

2] “Floor Failure Report” Dec 1997 by New Zealander Consultant.

3] Average Value of W/C from Building Research Authority NZ (Branz)

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